WATER AND WASTE TRENDS

Published in Pulp Paper International, January 2004

The timescale of these articles usually extends back to cover what's been happening on the water and waste front over about the last 12 months or so, but this time we are going back to what, for most mills, would have been the pioneering days some 50 years ago. It's likely that many mills will not be able to recall exactly what they were doing on the paper machine this long ago, let alone in terms of water and waste management, so I'm going to tell the story of a fictitious paper mill that has total recall of its history over this time. It does not matter too much where the mill is located, but let's assume that's it's somewhere in Europe within the EU. From well before the days of ISO 14001, EMAS and eco-labels, this company has always prided itself on setting its own agenda on environmental topics and, like many other mills, this began in the 1960s with its effluent. At this time, the mill had two paper machines making about 100 tonne/day of fine paper (printings/writings) from purchased pulp, clay, starch and rosin size.

The mill obtained (and still obtains) its fresh water from the local river, requiring only filtration and disinfection before use. With no real incentive to economise on water use at the time, the mill discharged some 10,000 m3/day to the river from a very open water system, but at least this kept the not inconsiderable losses of fibre, filler and starch (in total about 7% of production) down to concentrations of about 650 mg/l total suspended solids (TSS) and 50 mg/l Biochemical Oxygen Demand (BOD). Wastes were the typical mixture of old felts/wires, packaging, etc and went to the local dump.  The 1960s saw the start of the mill's pro-active approach to environmental management when it installed its first wastewater treatment plant. In order to reduce the size of the treatment plant, the mill had closed up its machines by simple measures like segregating clean/dirty streams and more internal recycling using in-line filters on return waters. Despite a 50% increase in production to 150 tonne/day, the water intake was reduced to 7500 m3/day corresponding to a specific water consumption of 50 m3/tonne. Together with slightly improved wire retentions, these measures lifted raw material efficiency up to around 97% leaving only about 3.5 tonne/day of primary sludge solids (in the form of a cake dewatered by a vacuum filter) to join the rest of the site waste going to the dump (see Figure 1).

At that time, sedimentation was easily the most popular option for primary treatment and the raw effluent settled well without the need for help from coagulants or flocculants due to presence of a useful excess of aluminium compounds left over from the use of alum within the process. Shortly after the start-up of the wastewater treatment plant, one of these irksome ironies that can befall the best-laid plans started to make itself felt. Up until that time, the river bed had been smothered in a mixture of papermaking fibres and fillers, which were periodically swept away after rainfall. All the settleable suspended solids were now removed leaving a slightly cloudy water with a low level of dissolved organics for discharge. Unfortunately, the make-up of the organics proved suitable as a food source for a particular microbiological community commonly referred to as sewage fungus.

Despite its name, this community is usually dominated not by fungi, but by bacteria. It has since been shown that these filamentous bacteria in the river can in fact only use certain types of organic matter within the BOD fraction, notably low molecular mass compounds such as glucose, the main source of which would be starches. Over the years, this problem has afflicted a good number of pulp as well as paper mills due to the presence of wood-derived degraded carbohydrates in wastewaters. It is a rather more intractable problem for pulp mills as it is difficult to eliminate such compounds by process modification whereas paper mills can attempt to do so my improving starch retention. After much chemical detective work, the mill showed that the mill broke with its high load of surface-applied starch was indeed responsible for the sewage fungus growth, albeit aided by the microbial action at the wet end which converted the non-available parent starches to available glucose and maltose. As a means of minimising this problem, the mill was one of the first to switch to cationic starch at the size press due to their better retention in recycled broke, but other benefits related to the cleaner wet end helped to compensate for their higher purchase price.

This measure reduced the effluent BOD to about 50 mg/l, but this improvement was made somewhat irrelevant a few years later by the mill's decision to broaden its product mix by converting one machine to the manufacture of packaging grades from recovered paper. As for other recycled mills at this time, the environmental aspect of this change (in terms of minimising the dumping of wastepaper) was not a major factor, but the mill did have to face up to the reality of using recovered paper in terms of site emissions. At this time, there was no practical alternative to the installation of an aerobic activated sludge plant to deal with the higher BOD loads, although the mill were concerned at the high energy/chemical inputs required and the high output of secondary sludge to add to the cleaning rejects. Biological filtration was rejected due to high land requirements.

The activated sludge plant selected was a typical design used at the time for industrial wastewater treatment, comprising a completely-mixed aeration tank with surface aerators, which is excellent for coping with BOD load variations from the mill. Unfortunately, this design is also excellent for growing within the treatment system the same type of bacteria that used to be in the river causing sewage fungus. As many mills have since found to their cost, these filamentous bacteria impair consolidation of the activated sludge (a problem commonly known as sludge bulking) and, without some form of control, cause the loss of biomass solids and eventually also of process efficiency in terms of BOD removal.

Not surprisingly, resource efficiency appeared to drop off with the use of recovered paper mainly due to the rejects from cleaning, which still contained a lot of potentially-usable fibre. However, the definition of resource efficiency needs a fresh look when what would be otherwise be a waste is re-used. Most of the primary sludge was being recycled to the packaging machine with just enough passing to the existing vacuum filter to ease the poor dewaterability of the surplus activated sludge (3-4 tonne solids/day). Overall therefore, about 6% of the mill's raw material input was not being utilised.

During the 1970s, the mill struggled along with periods of excellent performance giving discharge TSS and BOD concentrations below 30 mg/l, but interspersed with bad bulking periods that were difficult to control even with lime or chlorine dosing to kill off the undesirable filaments. The mill continued to expand, albeit with the  same absolute fresh water consumption and the higher TSS and BOD loads necessitated an expansion of treatment capacity. Although the existing plant could deal with the flow throughput, it was decided to replace the large primary sedimentation tanks with a more compact flotation system and also include a small flow balancing tank to deal with flow variations in the raw wastewater. The use of flotation improved the quality of the sludge so that it could be re-used on the packaging machine with no problems. The mechanical aeration plant was augmented with oxygenation and the opportunity also taken to retrofit a small aeration compartment ahead of the main aeration/oxygenation tank. Research had shown that such a tank could help the microbial population in the activated sludge select against the filamentous types and for the good floc-formers.

As with most mill modifications, a number of different things had been changed all at the same time so it was rather difficult to be unequivocal about which of these was responsible for the decrease in the frequency of bulking (but not its elimination) that followed. It was quite likely that all had contributed in some way - the more stable flow regime, the less anaerobic character of the primary effluent, the new selector tank and the absence of any pockets of low dissolved oxygen in the main bioreactor. The mill's change of direction away from printings/writings had improved its profitability and so the decision was made in the 1980s to convert the other machine to fluting/liner production as well.

From about the mid-1970s, a lot of research had been conducted on applying a rather old technology to the treatment of industrial wastewaters and this was what is now the well-known technique of anaerobic biological treatment, most commonly in some form of compact upflow reactor. Whilst aerobic treatment could be applied to wastewaters of virtually any strength, anaerobic treatment (at least at that time) required a reasonably strong, preferably warm, wastewater before it could be considered. An ideal candidate for this process was the wastewater generated at recycled packaging mills, which was strong and warm due to the very closed water systems and the high input of starch with the recovered paper. This was the obvious process, in the form of an upflow anaerobic sludge blanket (UASB) reactor, to fit in between the existing primary flotation unit and the activated sludge plant in order to cope with the increased BOD loads from the second packaging machine (see Figure 2).

Despite the greater use of recovered paper, which now represented the only fibre source, the overall raw material efficiency stayed constant at about 94% because of the continuing re-use of primary sludge and the use of the methane from the UASB process to replace purchased fuels. The wastewater treatment plant was very efficient in terms of overall removals, but the discharge concentrations were somewhat above previous levels due to the higher input loads. However, the mill was fortunate in having a regulator who recognised that discharge loads (rather than concentrations) determined the environmental effect in the recipient and that these were still on a declining path.

At the start of the 1990s, the mill foresaw a significant ramping up of interest in its environmental performance because of the general pressure on the paper industry stemming from the continuing concerns over chlorine bleaching and the specific pressure on packaging of all types. Although the mill had considered itself somewhat ahead of the times over the previous 20 years, not least in setting itself discharge standards more stringent than demanded by the regulator, it had not got round to formulating an official environmental policy. As soon as the then new environmental management system ISO 14001 appeared, the mill quickly realised that this provided an ideal framework to continue improving its environmental performance in all areas. As the mill also felt that it wanted to let people know what it had achieved environmentally, the decision was made not only to get certified to ISO 14001, but also to the EU's Eco-Management and Audit Scheme (EMAS) as this imposed additional reporting requirements.

On the production side, the mill also saw the opportunity to move into somewhat higher added-value grades such as white-top liners, which necessitated getting involved in the technology of deinking. It was envisaged that, with the better retention of dissolved substances like starch due to greater water closure, the existing biotreatment plant could cope with the extra BOD loading from the continuing higher production. This was born out in practice, but another contributing factor was the ability of the UASB system to operate at well above its original design loadings. Of greater potential significance was the big increase in sludge wastes to about 100 tonne/day, but the mill had been experimenting for some time with an alternative to landfill for its relatively small quantities of mixed primary/secondary sludges. This was the application of sludge to local agricultural land, which being somewhat sandy in nature, benefited from the presence of fibrous material for water retention, of calcium carbonate for its liming contribution and from the nutrient content of the biomass.

As the 20th century drew to a close, the mill could look back on nearly 50 years of manufacturing during which it had increased paper production by over an order of magnitude whilst at the same time turning its main raw material from 100% virgin pulp to 100% recovered paper and lowering its emissions to water (see Table 1 summary). It was also facing some new challenges in terms of legislation with the implementation within a few years of the EU Directive on Integrated Pollution Prevention and Control (IPPC) and the wider range of issues in moving to sustainable paper production. With the installation of more deinking capacity, the solid waste aspect became more critical and suitable local land for sludge application ran out as the mill were against trucking the sludge long distances. Local industries such as cement and brick manufacture had previously turned down the sludge (and rejects) as fuels due to their unacceptably high water content so the mill decided to do something about this. The old vacuum filters had already been replaced with screw presses and improved chemical conditioning and steam addition to the screw raised the sludge solids to about the maximum possible by this means (65% dryness). On the rejects, improved cleaning to lower the fibre content reduced the quantity and lifted its solids content to 70%, thus allowing both residue streams to be used as fuels off-site. The mill does not see this as the ultimate solution as it would prefer to be able to re-use these residues itself and is watching closely developments in filler recovery techniques.

The possibility of something similar has also suggested itself on the wastewater side due to the worsening problem of calcium carbonate precipitation stemming from inadequate control of acidification reactions within the machine systems. Some precipitation occurs within the biological treatment stages, but the wastewater is still unstable leading to rising TSS levels in the discharge and in the wastewater recycled to the mill. This problem has been partially solved by further aeration in a non-biological reactor, but it is recognised that this issue (plus that of other salts) needs tackling closer to its source within the paper machines. The future is thus likely to see greater integration of the wastewater treatment processes (probably new, more compact versions of what is being used already) within the paper machine systems allied to better circuit separation to route undesirable substances (ie anything water soluble) away from the thin stock and whitewater systems. Even together with the opportunities for in-house use of solid residues, the overall raw material efficiency figure cannot be bettered that much, but it should make achieving close to 100% utilisation more sustainable.  

 

Table 1 Summary of mill changes

 

 

Period

Paper

production

Freshwater

 use

River discharge loads (tonne/day)

Solid waste

to landfill

Raw material efficiency

Use of recovered paper

 

(tonne/day)

(m3/day)

TSS

BOD

(tonne/day)

 (%)

 (tonne/day)

1950s

100

10,000

6.5

0.8

0

93

0

1960s

150

7,500

0.33

0.66

3

97

0

1970s

400

10,000

0.34

0.5

24

94

200

1980s

500

2,500

0.43

0.34

35

94

530

1990s

1000

3,000

0.19

0.22

50

95

1130

2003

1200

2,400

0.1

0.1

15

99

1430

Note: Raw material efficiency defined as % of total papermaking raw materials being used beneficially in some way